王玺, 梅清晨, 贾禄冰. 价值流分析在连接器装配中的精益改善应用[J]. 制造技术与机床, 2022, (4): 154-158. DOI: 10.19287/j.mtmt.1005-2402.2022.04.025
引用本文: 王玺, 梅清晨, 贾禄冰. 价值流分析在连接器装配中的精益改善应用[J]. 制造技术与机床, 2022, (4): 154-158. DOI: 10.19287/j.mtmt.1005-2402.2022.04.025
WANG Xi, MEI Qingchen, JIA Lubing. Lean improvement’s application of value stream analysis in connector assembly[J]. Manufacturing Technology & Machine Tool, 2022, (4): 154-158. DOI: 10.19287/j.mtmt.1005-2402.2022.04.025
Citation: WANG Xi, MEI Qingchen, JIA Lubing. Lean improvement’s application of value stream analysis in connector assembly[J]. Manufacturing Technology & Machine Tool, 2022, (4): 154-158. DOI: 10.19287/j.mtmt.1005-2402.2022.04.025

价值流分析在连接器装配中的精益改善应用

Lean improvement’s application of value stream analysis in connector assembly

  • 摘要: 以A车间连接器装配过程为例,研究了利用价值流分析并结合精益工具对连接器装配过程的精益改善。首先通过现场调研写实,绘制出了现状价值流图,识别出生产中存在的不增值环节。其次,运用精益思想分析出布局物流不合理、生产模式落后、线平衡率低、在制品多和标准化水平低等不增值因素产生的原因。最后,综合运用多种精益生产工具方法,优化了车间布局及物流、设计了拉动式生产、推行准时化配送、线平衡改善及推行标准作业等,实现车间人均效率提升35.02%,生产周期缩短26.93%,在制品量降低26.78%。

     

    Abstract: Combined with value stream analysis and lean tools, the lean improvement of connector assembly process was studied in A workshop’s connector assembly process. In order to identify the non-value-added links in production, the current value stream mapping was drawn through field investigation firstly. Meanwhile, the causes of non value-added factors, including unreasonable logistics layout, backward production mode, low line balance rate, much WIP and low standardization level, were figured out by virtue of the lean thinking. Finally, with the help of various lean production tools and methods, it optimized workshop layout and logistics, designed pull production, implemented just-in-time distribution, improved line balance and implemented standard operation. It successfully reached that the per capita efficiency of the workshop was increased by 35.02%, the production cycle was shortened by 26.93%, and the WIP was reduced by 26.78%.

     

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